1988 Mazda RX-7 Turbo II
Home Automotive
Projects Articles For
Sale Photos Links
Current Upgrades:
Racing Beat 3" turbo back exhaust
Autozone intake with cold air box
Throttle body mod
Ported intake manifold
Emissions removed/simplified vacuum lines
BNR S5
Stage 3 turbo
Greddy Profec II EBC (9 psi low boost, 15 psi high)
20"x9" FMIC, 2.5" piping
RTEK 2.1 ECU
RC Engineering 750cc primary injectors, 1600cc secondary
Walbro 255 fuel pump
Greddy Type S BOV
AEM UEGO wideband O2
ACT lightweight flywheel
ACT M/M clutch disc, heavy duty pressure plate
Tein Flex coilovers
Slotted rotors
S5 TII wheels (16x7)
310 whp @13 psi
Future plans:
Steetported engine
Paint and body work
10/05/05
I had to drive to Moorseville, NC
to pick this car up. It is an 88 Turbo II with 185k
miles. Engine rebuilt by Bruce Turrentine at 150k
miles. Bought for $3000. It needs a little work, it
was leaking coolant and power steering fluid, has a few dents and needs
paint, idles a little low, and needs a new throttle cable. But it
was still a good deal, as Turbo II's are fairly rare and hard to
find. I will probably use the GXL as a parts donor for it.

10/25/05
Initially, the TII
needed a lot of work. I fixed the coolant leak. The lower
radiator
hose was not clamped down all the way, and was not in the best
condition anyway, so I replaced it with a new one. Every once in
a
while the coolant level buzzer/alarm would go off when driving, which
is very annoying. Congrats for Mazda for making the most annoying
buzzer sound ever. I cleaned the coolant level sensor and made
sure
there were no air pockets in the system, and it seems to have
worked.
Next, I flushed the oil; two oil changes in the same week, using
Castrol GTX 10W-30. There also was an exhaust leak, making the
cabin
smell like exhaust if you had the windows rolled down. I replaced
some
missing exhaust downpipe nuts, and the smell isnt as bad, but still
stinks, I guess because the emissions are removed. I also
rerouted
some vacuum lines that were not going anywhere. The idle was too
low;
it would stall when coming to a stop especially when not warmed
up. I
bumped it up to about 900 rpm. The emissions removal got rid
of some of the cold-start idle control, so I set the idle kind of high
so it wont stall out so easily. Some parts were swapped from the
GXL
too. The seats, back hatch window, S5 Turbo rims, exterior trim,
rear bumper, and some interior
pieces. Also painted the front bumper trim to match the car.
Also replaced the throttle cable, fuel filter, and changed the
tranny and differential fluid with Redline 75W-90 and MT-90 gear oil.
3/06
It broke down and left me stranded a mile from my house one night.
Left it there to fix it in the morning. The next morning I
found it broken into. The geniuses broke the passenger side
window and ripped out the stereo, leaving the $300 SAFC and the $100
turbo timer on the ground. The problem ended up being a blown
engine fuse, which was later found to be caused by loose/unshielded
fuel pump wiring. I dont plan on putting the SAFC or the turbo
timer
back in for fear of future thievery. Turbo timers are practically
useless for water cooled turbos anyway. I plan on
ordering the RTEK 2.0 ECU, which will control fuel mixture better than
the SAFC.

4/06
Started installing a FMIC. Bought an ebay intercooler, 9" by 20"
core, bar and plate type. Total costs: IC, $190; Higgi'sTB
adapter, $100; ebay 2.5" IC tubing kit, $120; various couplers and
mounting pieces, $30; 2.5" BOV adapter, $45; total: ~$500.
The Greddy "bolt-on" kit is almost $1000, so it definately
was a better deal making a custom setup. Also relocating the
battery to one of the interior bins for room for IC piping. I
noticed a 1 psi drop in boost pressure, but i suppose it is expected
due to all longer/bigger piping and bigger intercooler. It does
feel like its lost a little power, but that is because the stock turbo
is a little undersized for this intercooler.

5/06
I sent the ECU to pocketlogger for the RTEK 2.0 upgrade.
Got the ECU back a week later. The 2.0 upgrade includes
fuel and timing tunability, as well as sensor readouts and built-in
720cc injector presets. Also ordered an AEM UEGO wideband oxygen
sensor to tune with. I took it out and did a few test runs with the
fuel map set for stock, logging the AFR with the rtek, and found out it
was running in the mid 12's, which was a tad too lean for me. I
was aiming for low to mid 11's under boost to be safe. As it
turned out, I had to set the rtek for +15% correction to get the AFRs
down in that range. I have not messed with timing; I dont really
know much about the timing effects.
7/06
Installed a cold air box
for the intake. The box was made from a sheet of aluminum which
worked out really well. It made a big difference on the AFM temp
sensor (using RTEK readouts).
11/06
Finally got around to fixing the front fender. It was hit-and-run
in a parking lot a week after I bought it, leaving a nice big dent
right over the front right wheel. I rattle-canned the new fender
white until I can get a decent paint job for the whole car.
6/07/08
I have not updated this in a while, but the car has had a lot of
progress. I upgraded the injectors to RC Engineering
750cc primaries and 1000cc secondaries. The 750cc primaries
are high impedence, so no in line resistors were needed. The
1000cc secondaries are low impedence, so 6.2 ohm resistors were wired
inline. I also rerouted the intercooler piping to reduce bends;
it is down to four major bends for minimal turbo lag. I also
finally sent the turbo to BNR Supercars
for a Stage 3 overhaul. This replaced the stock compressor side
with a 60-1 compressor in a T04B housing. The exhaust side is
kept stock except for clipping the wheel for less backpressure and
porting the wastegate to 35mm.

Since then i have had it to the dyno several times for tuning.
The 750cc/1000cc injector combo seems to small for the setup.
I was hitting 90% duty cycle at high 11's AFR. Check out
the dyno plots:
This was on the stock turbo at 9 psi; the boost dropped to 6 psi by redline:

This was just after installing the BNR Stage 3. Boost held steady at 6 psi wastegate pressure to redline:

This was a few weeks later, after installing an electronic boost
controller. This run was at 12 psi, with very conservative timing.

As you can see, the AFRs were fairly
lean. I replaced the 1000cc injectors with RC 1600cc later on.
Shortly after the new turbo, the coolant seals started showing
leakage. It still starts and runs like normal, but you have
to top off the coolant regularly. A replacement S4 TII block was
rebuilt by RX7world, with Rotary Aviation 2mm Super Seals and a mild streetport.

I still have not installed it yet; i would like to get the tuning
finished on the old engine. I also ordered a full set of Tein
flex coilovers; the handling was improved immensely. It is very
stiff, but if feels like a go cart in the turns.

The old brake rotors were also upgraded to slotted type all around with
new brake pads. The first two pics are of the old rotors; take a
look at the trenches dug into them. A previous owner forgot
a washer on one of the caliper mounting bolts, and it was making
contact with the rotor.

Lastly, a few cosmetic items were installed: used stock S5 TII sideskirts and an S5 TII replica lip from JKL Engineering.

The next things to do are install the new engine and send it off to a body shop for dent removal and paint.