S/V FAST BREAK

 

MAINTENANCE and IMPROVEMENT RECORD

 

 

 

06 – 10 NOV

 

Bend on Hood Main and take Manchester Main to sailmaker for repair of the problem involving the sticking slugs.

 

14 – 15 NOV

 

Replace Secondary (engine-mounted) Fuel Filter (OEM / YANMAR).

 

Replace Primary Fuel Filter: Install RACOR R230R2 Filter & R20S Element.

Upon removal, the (originally fitted) FRAM fuel filter appeared to contain only a minimal trace of foul-smelling mung which I suspected was deteriorating rubber from a washer or seal or hose or else a trace of dead algae. I detected no water in the filter. All this after having been assured by the Newport, RI Yanmar dealer that I was certain to acquire some water-contaminated fuel on the delivery and that this would make it necessary to change the filter element at least twice before I reached Florida. The primary motivation to change from the FRAM to RACOR was to acquire an enhanced capability of monitoring the intake of water and other contamination and an ease of serviceability and replacement.  

 

21 NOV

 

Service Raw Water Pump: Inspect & Retain Impeller. The impeller looks brand new. It now has no less than 230 hours on it (including approximately sixty in Wayne’s 2000 season if he had it changed out this spring), some of which involved running it dry for a total of no less than 20 minutes, and a fair amount of which involved running in “silty” water. There are no signs of wear or deterioration such as cracking of the vanes near the hub or abrasion of the tips of the vanes. It appears as if it could be relied upon for another 250 hours at the very least. I was promised in no uncertain terms by Mike at the Yanmar dealer in Newport, RI that I would find it necessary to replace the impeller at least once on the delivery. Oh Well.

 

Finish Re-plumbing Electric Bilge Pump: Pump hose now re-routed and fitted with check valve in bilge.

 

22 NOV

 

Replace spinnaker sheet snap-shackles with larger ones; cut and re-splice sheets and fit braided lanyards to shackle pull rings.

 

24 NOV

 

Re-fit washed air cleaner.

 

27 NOV

 

Bend on Manchester Main after sailmaker’s

1)      replacement of slides with longer-bodied slugs,

2)      fitting of chafe patch at points-of-contact with spreaders and

3)      cutting slits in foot to accommodate reefing earring passed around boom.

 

Install refurbished two-burner Origo alcohol stove.

 

30 NOV

 

Adjust Stuffing Box.

Install support brackets for ½ bulkhead shelving in salon.

Replace aft starboard N/F ventilator ring with pull-ring fitted to insert.

 

02 DEC

 

Replace zinc collar anode on prop shaft.

Finish reconnection / refurbishment of holding-tank plumbing  (head and pump-out hoses)

– began on 24 NOV.

Finish reconfiguration of cockpit locker stowage and access to shaft log from port.

 

06 DEC

 

Affix FL 9197 LK and FL State Vessel Registration Decal to forward topsides (P&S).

Replace aft port N/F ventilator ring. 

 

12 DEC

 

Finish upgrading bracing for holding tank (which now will not move, as in “slide”, aft without the bracing being removed).

 

17 DEC

 

Re-installed 14 gallon fresh water tank (now fitted with a 6 inch inspection plate) and its associated plumbing and installed Whale hand pumps in the galley and head.

 

03 JAN

 

Repair compass illumination: inoperative since purchase of boat.

 

 

09 JAN

 

Remove a “birds nest” from inside the mast – must have been put there in the winter-spring of 2000 and not noticed when the mast was stepped. Discovered it totally by surprise when fishing around inside the stick with a coat hanger probe through wiring holes in an attempt to start on restoring the foredeck light to service. Quite a surprise – could have “knocked me over with a feather” so to speak, Ha Ha!!   

 

11 JAN

 

Finish re-installing refurbished manual bilge pump.

Complete installation of GPS/PC interface and 12V DC power hook-up.

 

16 JAN

 

Remove the roller furling drum from the forestay to provide less obstruction to sailhandling and reduce chafe at the foot of the headsail. The drum was inoperative and had been installed only to receive PHRF rating credits.

 

17 JAN

 

Repack the stuffing box; replacing the old grease-impregnated flax packing with a newer type of synthetic grease-impregnated teflon-based fiber packing used in conjunction (as the ends of a sandwich configuration) with a moldable “drip-free” packing. The constantly dripping box is now bone dry at rest and is supposed to remain that way while turning as well. The box is very warm to the touch but that symptom is supposed to disappear as the packing “beds in”. The shaft is scored already but what can one expect after 15 years of service. Hoping for the best.

 

Replace the pull-ring handle on the icebox lid – broken since the acquisition of the boat.

 

26 JAN

 

Install new VHF and antenna (on sternrail).

 

01 FEB

 

Replace forward N/F ventilator ring with new one.

Fit newly acquired N/F 24-hr solar powered ventilator to forward ring.

 

04 FEB

 

Replace old warped stained wood propane locker lid with new gray “Starboard” lid.

 

 

 

06 FEB

 

Replace sea strainer-to-water pump ½” OD barb with 5/8” OD barb to match water pump diameter and remove flow restriction.

 

07 FEB

 

Rewire sidelight wiring in forepeak – replacing wire nuts with bus-bar and removing taped loops which dangled and threatened to snag or be strained during ground tackle evolutions.

 

10 FEB

 

Replace foredeck illumination bulb in mast-mounted combination fitting. The bulb was burned out since the acquisition of the boat.

 

Secure throttle/shifter mechanism to cockpit side with thru-bolts – replacing OEM lag screws which were working loose and contributing toward making shifting difficult.

 

Change OEM sea-strainer cover gasket with new one to improve ability to seal strainer and water intake system with less load on strainer cover wing-nuts.

 

Replace prop shaft zinc collar anode. Previously installed unit fell off due to inferior installation technique.

 

17 FEB

 

Install Clinometer below engine instrument panel.

 

26 FEB

 

Acquire used Dacron #3 in exchange for used Kevlar #3 and $500 cash – have reef points

installed. The sail is approximately 5 years old and has been used no more than ten times and the

exchange provides me with enough cash to have the reef installed. The reef reduces the 194

square feet by approximately 43 square feet to 150 square feet. 

 

07 MAR

 

Fit new lifelines; uncovered 3/16” SS 1X19.

 

12 MAR

 

Install tangs on mainsheet boom bale bolt in order to anchor reefing earrings without torqueing

the bale forward.

 

 

 

14 MAR

 

Finish replacement (and resealing) of 4 main cabin deadlights – began in January.

 

08 – 12 APR

 

Finish scraping all stain and varnish from exterior teak – began in early March. All exterior

wood is now natural teak except for the tiller (varnished ash).

 

Fit new cunningham with a narrow profile (due to use of fiddle blocks) and a 4:1 purchase.

 

Fit an acrylic (plexi-glass) book retainer to the starboard shelf in the salon area.

 

19 APR

 

Haul Out

 

21 APR  

 

Drill out lifeline stanchion base plates for ¼” fastenings.

 

Re-engineer the fastenings which hold the boom to the gooseneck fitting. Two out of three of the

OEM fastenings had sheered or stripped the threads in the gooseneck and the third was galled

into its hole and had to be drilled out in a vice. During the process the up-down pivot bolt and the

side-to-side pivot pin were examined, cleaned up and lubed and the interior of the boom was

evaluated for the feasibility of hardware installations such as jiffy reefing eyes. This repair began

16 APR.

 

Install new optical domes, expansion diaphragms and large and small O-ring seals in both

compasses. The port compass continued to lose fluid after a January repair due to a leaking dome

which was discovered only after a very close examination upon the reappearance (after 8

weeks) of the bubble. The repair took 14 days as a result of Ritchie Navigation sending me the

wrong domes the first time. The repair was otherwise easily accomplished in spite of Ritchie’s

dire warnings of the difficulties associated with the re-assembly of the compasses and the strong

recommendation to prevent problems by utilizing a Ritchie-authorized service shop. 

 

Remove lifeline stanchions and (at residence with the aid of extensive use of a propane torch)

remove zamac top fittings for eventual replacement.


 

22 APR 

 

Inspect mast and restore swivel capability to deck-level halyard sheaves. Replace halyards with messengers.

 

Remove chainplates for eventual replacement with parts that have already been acquired.

 

Remove tiller in preparation for refinishing and installation of new hiking stick.

 

At residence, drill out lifeline stanchions and tap ¼” x 20 threads into stanchion bolt holes. Also remove rust and damage to finish from propane torch and polish the stanchions with buffing wheel mounted on bench grinder.

 

23 APR  

 

Ship halyards to Layline to renew splices and evaluate lines for remaining serviceability as a result of UV exposure and chafe. Lengthy discussion on rigging subjects with Henry Mallard, another J/30 owner who works there and made up the original running rigging order for Wayne in 1998.

 

Remove headsail halyard sheave exit box from mast and ship it to Rig-Rite for replacement of the lower jib halyard sheave which was binding once per revolution with a clicking sound like a ratchet. This was probably from the deformation of the sheave pin as a result of the continuous strain of a permanently tensioned roller furling (by the first owner).

 

Muck-out port chainplate hole in the deck for eventual replacement of crappy core with WEST epoxy putty.

 

24 APR 

 

New name, hailing port, FL State registration numbers, boot and cove stripes installed – blue instead of green or black. The boat is now trimmed in blue wherever it was formerly green.

 

 


 

25 APR   

 

Remove the upper and lower segments of the spinnaker pole track from the mast. All of the fastenings will be replaced. In the lower segment, ¼” x 20 RH screws were used which will now be replaced by 5/16" x 18 FH screws after the holes are drilled out and tapped properly.

 

Push WEST epoxy/Cabosil putty into the area of the port chainplate hole in the deck where the core had become degraded as a result of the entrance of water. 

 

Attempt, partially successfully, to remove spilled epoxy from the areas of the bulkhead and deck where a prior effort at repairing leaking chainplates had resulted in the epoxy pouring down from the deck opening prior to curing.

 

Strip the tiller at the yard and apply the first two coats of WEST epoxy at home.

 

Polish the chainplate deck hole covers at residence.

 

26 APR 

 

Acquire new standing rigging and Tuff-Luff from sailing Services, Miami.

 

Acquire from Sailing Services new cylindrical stainless steel (instead of conical Zamac) tops for lifeline stanchions.

 

Complete preparation of chainplate areas on deck and in cabin for installation (bedding and bolting) of new chainplates.


 

27 APR 

 

Install new chainplates with 3M-101. That was what was formerly used and there is no way to correct the tendency to develop deck leaks at that fitting, the only recourse is to change the compound frequently (annually).

 

Remove the cabin/head door from the boat. This should make movement through the boat easier and enhance access to the hanging locker space to starboard of the head compartment. The door has not been used for the purpose of providing privacy since I purchased the boat but it has definitely distracted from the focus of maintaining a clean hanging locker area and permanently improving the function of it. We’ll see how this works out. The idea to remove the door came as result of the temporary requirement to dismount it in order to be able to handle tools on both sides of the main bulkhead in the course of replacing the chainplates. It is a quick-pickup pintle-gudgeon arrangement as I discovered after needlessly unscrewing the first hinge (gudgeon).        

 

Complete spinnaker pole track upgrade as described in 25 APR entry. The lower segment is now secured with 5/16” FH SS machine screws. The upper and lower segment screws are now all Phillips head (they were formerly slotted) and are all secured with thread locking compound. Burrs which impeded the movement of the cars have been filed off the upper segment and the cars now move much more freely.  

 

30 APR

 

Completed compounding and waxing the mast. Began on 29 APR.

 

New 5/16” SS hex bolts securing the tiller to its SS cheeks/straps were cut to length (3 1/4”).

 

01 MAY

 

Re-install headsail halyard sheave box.

 

Fit new Tuff-Luff system (plastic extrusion and SS fittings) to headstay (maximum fanfare and hassle in spite of instructions – 4 hours; this should be done only with the mast stepped).

 


 

02 MAY

 

Bottom maintenance (began 25 APR) was completed by Pollon Services. The keel was taken down to lead wherever there were blisters (this involved a 2’ X 2’ section on port and several palm-sized areas on starboard) and then filled and primed. The bottom was sanded and painted with Interlux Ultra.

 

The topsides gelcoat was compounded and waxed by Pollon Services/Neet Fleet (began 29 APR).

 

Fit new standing rigging to mast.

 

Re-reave all halyards and spinnaker pole topping lift (the latter took 3 hours instead of 10 minutes- what a disaster; lost the messenger and the whole works).

 

Complete fitting new socket for tiller extension. This began on 20 APR and required the structural reinforcement of the wood near the socket with fiberglass tape wrapped around the shaft of the tiller – quite a production. Additionally, the tiller was coated with 2 coats of WEST epoxy and 4 coats of Z-spar 1015 varnish.

 

New tiller pivot bolt (1/2”`X 13 X 3 1/4” SS Hex bolt) was acquired.

 

Fit new masthead mounting bracket for Windex – fabricated from scrap SS sail track found on the ground in the area of the mast storage. This was made necessary by the larger sized marine eye on the new backstay preventing the original hole in the crane arm from being used and was a desperate response which ironically represents an improvement in Windex visibility, serviceability and engineering.  

 

03 MAY

 

Remove lower rudder pintle strap and remove rust from it and polish it before replacing it with new SS bolts (the originals were very rusty) and bedding it with 3M –101 instead of silicone as was done by the factory. Additionally, the bedding surface (for the pintle straps) of the rudder was scraped and compounded until almost all the rust and rust stains were removed and the pintle pins themselves were also similarly reconditioned.

 

Step mast and complete fitting of new standing rigging.

 

04 MAY

 

Launch

 

 

 

 

 

07 MAY

 

Bend on Mainsail and fit new blue Sunbrella sailcover.

 

08 MAY

 

Re-fit lifelines and fit new SS cylindrical stanchion caps to replace original Zamac conical caps. Also, the stanchions are now secured to the bases with ¼” X 20 SS machine screws instead of the original 3/16” SS machine screws.

 

09 MAY

 

Acquire second book retainer for salon shelf.

 

Acquire luff tape panel with grommets to secure Tuff-Luff from excessive oscillating in strong breezes when unused.

 

Perform first thorough cleaning of the hanging locker area.

 

12 MAY

 

Make significant progress toward a thorough cleaning of aft section of engine compartment sole. This involved scraping and scrubbing of spilled catalyzed adhesives or sealers and baked deposits of a compound of packing grease and salt around the area of the water-lift muffler and the shaft log/stuffing box.

 

Cut away more of the top of the aftermost bulkhead which continues to work very noisily (and most annoyingly) against the underside of the cockpit sole when beating to windward on port tack. This in spite of previous attempts to cut away the contacting surface.

 

15 MAY

 

Complete installation of Spar-Tite molded rubber mast wedge replacement system. Began on 12 MAY. Poured the rubber on 13 MAY.

 

24 MAY

 

Complete installation of Raytheon ST-2000+ Tiller Pilot. Began on 12 MAY.

 

Mount a LifeSling in a rigid container on the starboard quarter of the sternrail.

 

04 JUN

 

Replace prop shaft zinc collar anode.

 

 

06 JUN          

 

Fit buntlines (but they are not tied into the sails) for two reefs in the Main and one reef (including the tack pendant) in the #3.

 

10 JUN          

 

Replaced companionway slide track with new section obtained from TPI. The original had deteriorated from age (cold and UV) and abuse such as the weight of anyone furling the Main. A real pain-in-the-ass job requiring the infinite patience of John Nichols to complete properly.

 

Mounted a LifeSling in a rigid container on the starboard quarter of the sternrail.

 

Replaced rusted bolts holding engine instrument panel in place.

 

11 JUN          

 

Changed Crankcase Oil and Filter.

 

Serviced the batteries (the electrolyte was at the full level, none was added).

 

Inspected and drained the RAYCOR (primary) fuel filter. No water or sediment of any kind was present.

 

Attempted to repair the fuel leak which appeared to be originating from the fuel pump end of the fuel line between the RAYCOR (primary) fuel filter and the fuel pump. The leak may have been at the “banjo bolt” fitting into the fuel pump from the fuel line – the bolt “gave” a little bit and tightened up when I used a wrench on it (I am most reluctant to really “muscle” it). I also replaced the fuel line itself; in the process, reducing the I.D. of the line from 5/16” to ¼” which made the ends of the line fit more snugly on the barbs.

 

17 JUN          

 

Fit a ½ board into the upper panel of the companionway in order to minimize rain and spray ingress during certain periods of heavy weather when ventilation or cockpit-to-cabin communications are required.

 

13 JUL

 

The #1 Genny was repaired at UK Rhode Island for $135.00. The leech had torn away from the upper portion of the sail for approximately six feet, probably as a result of spreader chafe, leech flutter, rough handling, old age or a combination of any of these things. The leech is now approximately eight inches inside of its former position.

 

16 JUL

 

Replace after starboard lifeline stanchion which was damaged in a collision in a race on 14 JUL. I picked up the stanchion from Rig-Rite in person after a long walk from Apponaug Harbor to “downtown” Warwick. Cost = $75.00.

  

13 SEP

 

Service Raw Water Pump: Inspect & Replace Impeller. The old impeller looked brand new. It now has no less than 500 hours on it (including approximately sixty in Wayne’s 2000 season if he had it changed out in the Spring of ‘00). Again, as in November of last year, there are no signs of wear or deterioration such as cracking of the vanes near the hub or abrasion of the tips of the vanes. It appears as if it could be relied upon for another 250 hours at the very least. I changed it because I just didn’t want to think about it any more or have it fail at an inconvenient time on what remains of the delivery.

Replace Water Pump faceplate brass Phillips head screws with stainless hex screws.     

 

14 SEP

 

Repack the stuffing box; replacing the synthetic grease-impregnated teflon-based fiber packing installed in January with grease-impregnated flax packing which was all that was available in Georgetown, SC. The “drip-free” packing was great while it lasted (approximately 225 - 250 engine hours) but it quit in a hurry; going from fine to totally unacceptable in approximately 30 – 40 engine hours.

 

25 SEP

 

Have Main repaired at North Sails, Ft Lauderdale – the luff slug grommet above the first reef tack cringle had ripped the luff as a result of its being positioned to close to the cringle. The repair consisted of refastening the luff to the luff rope, setting the first luff slug grommet higher up the luff and setting a cringle for the Cunningham just above the reefing cringle – this last item actually being an improvement and not a repair. 

 


 

28 SEP

 

Replace the fresh water circulation pump which had begun to throw water out of the “trouble” hole during the last days of the delivery and which felt “loose” as a result of a possible failure of the non-serviceable bearing unit (a result of over-tensioning the pulley belt and/or the expiration of the serviceable life of the bearing. A messy job but one that was done right the first time with parts from Sun Power in Ft. Lauderdale.

 

30 JAN

 

Install new cylinder assembly on head pump. The old one was leaking due to a break in the plastic near the base where the cylinder mounted to the base. The repair process (disassembly, diagnosis, acquisition of replacement parts and reassembly) began on 28 JAN.

 

Remove port bulkhead compass – leaking again. The compass will probably be replaced by a self-contained solar-powered digital fluxgate unit when the funds are available but for now the bulkhead hole is patched with a “starboard” cover.

 

08 FEB

 

Re-lead GPS antenna cable and VHF antenna cable through the stern running light fitting on the sternrail and into the sternrail tubing to the units belowdecks. This replaces the clam through-deck fitting and the exposed wire-tied-to-the-sternrail stanchion installation with a much “cleaner” setup which should reduce the chances of the antenna wires being slugged or torn during the occasional “mayhem” in the transom area. This work on this improvement began on 01 FEB.   

 

23 FEB

 

Remove the fuel tank inspection plug/port after breaking galled threads loose with a special tool made by RJN – 02 FEB. The plug/port had been galled shut since OCT ’01 when I over-tightened it during a refueling in Melbourne, FL. It was necessary to remove the plug in order to be able to eventually perform a periodic cleaning of the tank and its fuel. Replace the galled fuel tank inspection plug (OEM) with a PVC plug.

 


 

12 – 14 MAR

 

Replace forehatch – removing the leaking (as a result of the top being bent – probably by a sheet or spinnaker pole in a racing accident) Lewmar Coastline model hatch with a much more substantial (but higher profile) Lewmar Ocean model hatch. The old fastening holes (from two installations –an OEM installation and the Coastline installation) were drilled out and injected with epoxy prior to the hatch being bedded in 3M-101 and fastened in place with #10 X ¾” SS FH self-tapping screws. The Coastline model hatch was cannibalized for extra parts from the hinges and dogs.

 

Replace sealing gasket on the Lewmar Coastline model hatches in the head and salon.   

 

Remove and re-mount the Whale fresh water pumps in the galley and head – upgrading their mounting on small “starboard” pads which now cover the holes left in the counter tops when the hot-and-cold faucet sets were removed. This project was started in early February and involved inferior craftsmanship and flawed pattern-making skills or it would have been completed much earlier.

 

17 MAR

 

Replace prop shaft zinc collar anode.

 

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