PROJECT X

Here's the story, click on the hypertext to see some pictures!

The completion took one and a half years to finish, and lasted less than 24 hours:

It all started as a dream. Something that I didn't think was done before (I found out that they're out there, just not many people know about them). What? A turbocharged Toyota Corolla GT-S (old school 1985 rear wheel drive model).

While a student at UC Davis, I had the opportunity to take, "Field Equipment Maintenance." Don't let the name fool you. It may have started out as a class for repairing things like tractors, but this was nothing more than a beginner welding class in disguise. That's when the idea started, and the clock began ticking. While I was taking welding, a few of my friends took advantage of my access to the welding equipment, and had me build some stuff for their cars (see TurtleSpeed Racing Products).

This page is about my project though. I started with the exhaust manifold. I saw a picture of a GReddy Stainless Steel turbo manifold in a Japanese magazine called Options2. I tried to build mine the same way. One bad thing...it was an equal length manifold and the picture I had to follow was a lot smaller than the one that I have now.. I think it would have been a lot easier to make a regular manifold (which is why most of the manifolds out there aren't equal length), but I wanted it to be just like the GReddy one (duh). I thought I was somewhat successful in copying the manifold except for the #4 cylinder which I couldn't see in the picture. The result was that I couldn't figure it out, and the #4 extractor is a really short piece that just bends right up to the turbo flange. Now that I've seen a bigger picture of the manifold, I see that mine is nothing like it. Oh well.

After finishing the manifold, I bolted it in, and discovered that it was too close to the engine block. It wouldn't sit properly because it would hit the oil filter that mounts right below it. I ended up cutting all the way across the top of the manifold, at the flange, and extending each extractor about one inch. I then tried it again. It was good this time and cleared the filter.

The next problem that wasn't thought out too well was the fact that the oil filter would NEVER come out with the new manifold because the way the bends are. The filter would be blocked in when the manifold was in place. I consider myself somewhat "hardcore" about my car, and all my friends definately think I am, but I wasn't about to take out the manifold every 3,000 miles just the change the oil filter. I wasn't too worried because I planned on getting a remote oil filter unit so that the filter would be somewhere else anyway.

I started sweating when I couldn't find a kit that fit my car. I lucked out when I joined the Toyota-Mods Mailing List. It's the absolute "must" for any Toyota Performance Ethusiast. The people on the list are nice, and someone will have the answer to any question you could possibly have. From there, I discovered CAP (Cyberspace Automotive Performance). They've got awesome prices, and a huge selection of stuff that's hard to find. If you've got a Toyota, and you're looking for something, check them out first, before you shell out the big bucks at some local Speed Shop.

In all, my "kit" consists of:

IHI Turbo with internal wastegate
CarTech Adjustable, Boost Variable Fuel Pressure Regulator
HKS Race Blow-Off Valve
1989 Supra Turbo Intercooler
CAP Remote Oil Filter Kit
JC Whitney Boost Gauge
CyberDyne Air/Fuel Ratio Gauge
Various sizes of piping and steel braid line


Then, I started building the piping. First I made some brackets and front mounted the intercooler. I bolted in the manifold, the turbo, and started making the piping from there. I wanted to keep everything in the engine bay that came with the car (cruise control, power steering, etc.). A distributorless ignition would open up mass amounts of space, and junking the cruise control would have been good too, not to mention dumping the powersteering, and losing the reservoir for the powersteering fluid, moving the battery to the trunk (you get the idea).

Building the piping was actually pretty fast...the bastard was making the downpipe. Since I tried building an equal length manifold, it was a tight squeeze making the pass between the steering joints, the firewall, and the frame of the car because of the twisting bends that the manifold had, taking up a lot of space. What little space was left, didn't leave much for imagination. I was able to kind of finish it up, but it was a monster creation.

I stress relieved the manifold at a place I found in the phone book called ThermoFusion in Hayward, CA. What that involved was heating the manifold to a high temperature, holding it there, and slowly cooling it so that all the molecules in the metal line up and are happy. What happens is that when you weld something, the part that you're welding gets hot, but the rest of your work-piece stay relatively cool. This disparity in temperatures makes the molecules in the metal unhappy, and the piece is weak.

I had a friend with a turbo Mazda MX-3 (4-cylinder). His custom (read as $$$) manifold cracked all time and he had it ceramic coated also. I think this was partly due to poor bracing of the heavy TO4 turbo, and partly might be due to the fact that the manifold wasn't stress relieved after it was finished.

Beyond stress relieving the manifold, I did plan to get it coated at JetHot, but held off because I figured that it might be a waste of money since I expected/am expecting the manifold to crack since I used pretty thin piping. 16 gauge mild steel was the only stuff I could find at the time I was building everything when I was a student at UCD. I since learned (from the Toyota-Mods List) that U-bend steam pipes are much stronger. Maybe I'll hunt some of those down in the future.

Yeah, building a turbo kit doesn't sound like much, but try doing all this while you're a full time student taking 16 units in undergrad, then studying for the LSAT, and then being a first year law student. All the while, you don't have anything to copy (unlike the mobs of Honda and Acura turbo kits that I could have copied if I had a Honda or Acura) The completion was planned for the summer of 97, but that fell through when my motor decided to throw the crankshaft pulley...twice. The second time, stripping the threads, and jacking my crank. As any true car buff would do, I turned the misfortune into an opportunity to spend waay too much money on my car!

As most car buffs have probably done, and if not, at least thought about doing before they were saved by a moment of rational thinking, I pulled a "Well, since I'll have to pull the motor out to replace the crankshaft with a new one, I might as well:"


Port and Polish the intake manifold
Pocket Port the head
Shot Peen the rods
Replace the rod and main bearings
Replace the valve springs
Polish the crank
Balance the motor
Lighten the flywheel
Replace the rings (HKS)


Yes, I like it, and yes it was bucks to do. Only problem I've had (although it's a big problem) is the fact that my car burns MAJOR oil. After running it by the Toy-Mods List, I've decided that it must be the oil rings. I installed HKS rings, which I was told, were chrome. I was also told that chrome being a harder alloy, has a harder time seating. In any case, the motor comes out again at Spring Break, for another ring job. This time, I'm putting in stockers.

Anyhow, back to my turbo story, finals came and immediately after the last one, I was back to my apartment to pick up the parts that had been collecting dust for a year and a half, and drove to my friend's shop, Import Circuit Tuning - ICT, where my install began. Oh yeah, I neglected to mention the headaches I had trying to match fittings for the turbo's oil feed and drain. Lucky for me, IHI supplied the old Mazda MX-6, and I was able to get the fittings from an old MX-6 Turbo. Then I had a bastard time getting fittings to T off the remote oil filter lines so that I could feed the turbo. I won't go into details, but trust me, it was a nightmare.

So in the kit went. Some of the piping needed to be crushed slightly since it didn't clear the hood as well as I remembered. I think extending the manifold extractors moved everything just enough so that the piping didn't clear perfect. I finished the downpipe leaving big time exhaust leaks. To make the story short, I was jetting around at 3.5-4 psi. The feeling is incredible. It's not that my car was some pocket rocket, but it's the feeling that I got when I heard the air in the turbo spooling, and the car beginning to pull faster than what I "knew" it should be pulling. That's about all I can say to describe the feeling. I'm sure some of that comes from the fact that I've had the car for years before I put the turbo in.

Well, I decided that the exhaust leaks were too big to keep the turbo in the car since the car was loud, and the car stunk when idling. I took everything out the next day after driving around and running some errands giving it a lot of thought. When I pulled the turbo off, all the intake piping from the turbo to the throttle body was filled with oil, and I had remembered seeing mass amounts of smoke in my rearview when under boost earlier in the day (another reason I decided to pull the turbo). The problem is either faulty oil seals, the oil drain line wasn't direct enough, or my oil rings. I'm thinking it's probably the latter two reasons.

That's the basic story, here's some pictures from the one day that the turbo was in my car. Oh well...it'll be back in there soon...hopefully.

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UPDATE: 7/8/97

Blew the motor. I guess that smoking was bit more of a problem than most people thought. I was driving the car back from LA, after visiting a friend, when I noticed that I was burning big-time oil. About a quart every 1/2 tank of gas...not to mention the smoke whenever I accelerated.

This sucks. I pulled the motor again, and it was pretty ugly when the shop took the lower block apart. I had three pistons showing damage, and one piston had the ring worn into the piston itself. Chips, and cracks everywhere. This lower block is history. I kept the crank, I don't know if it's usable...I'll have it check if I ever decide to try and use it again. It's fully balanced, and polished.

Got a used motor from Attarco down in the Bay Area. I decided to pull the head and to use my ported one instead. At that time, I decided to get another oil pan too since the one I welded for my drain fitting for the turbo was leaking. Then I just bolted everything up and dropped the motor in. Boom, fired up and I'm driving again.

The guys that tore the engine down told me that the rings were really loose, so maybe I got the wrong HKS rings. We'll never know. The turbo will have to wait.

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UPDATE: 9/18/98

It's been a while since I've updated. In the mean-time, I sent my manifold to a friend of mine. He knew someone with access to a milling machine at UC Davis through the engineering department. I never got to use the good machine shop because I wasn't an engineering student (although sometimes I wish I was and think I am).

Anyway, I sent my manifold to get the flange milled flat because of all the exhaust leaks coming from the manifold from the first time I put the turbo in. It was gone for about 6 months or so. I started wondering if my friend's friend had graduated and either: (1) took the manifold with him (2)lost it or (3)chucked it. Lucky for me, the guy was just really busy with moving apartments and he also had a hard time rigging the manifold up because it's got all the weird bends because of the attempt at making it equal length.

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UPDATE: 3/25/99

Turbo was put back into the car. I rewelded the downpipe at the areas that were leaking. The exhaust leaks are a lot smaller, but they're still there. I'm getting about 5.5psi of boost now. Only problem is that I'm smoking a lot when I'm under boost. I'm going to run it by the people on the Toyota-Mods List.

In the meantime, I went to a muffler shop and had them redo part of the downpipe. Since the fitting is so tight, the last time I had the turbo in the car, I couldn't complete the welding on the downpipe. I just did it enough to make the pipes connect, but they were leaking a lot of exhaust. Muffler Tech put in my flex pipe and changed the pieced-together piping as far as they could reach with a single pipe. They offered to do the whole downpipe if i brought it in...maybe later. Ditto with the 3 inch cat-back exhaust they offered to build me.

Well, I can't live with the smoking under boost (it's a lot), so I took it all out again. I'm pretty good at this now.

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UPDATE: 4/12/99

After pulling the manifold out, I noticed that it was leaking exahust gas all along the bottom side. It's not sitting flat against the head. The support brace that I have on the manifold isn't fitting right anymore since the flange was milled. I cut a piece off the support bracket (where a bolt connects it to the block), and hopefully, it'll sit on a bracket and move about somewhat freely while still supporting the turbo and manifold.

I put it all back in again. I tried to sand the downpipe flange but it's not perfectly flat. Through the recommendations by people on the Toyota-Mods List, I tried pulling the hosing that runs between the intake manifold, and the cam cover on the head. The theory is that the boost is pressurizing the head, and causing oil to get into the combustion chamber, causing the smoking under boost.

I plugged the manifold, and put a breather on the head. WOOOSSHHH! Stan's in business. I'm not smoking under boost anymore, but I am getting little puffs of smoke between shifts. I drove the car for about two days, and went back to the Bay Area to visit my family and to go to the AutoX at the Oakland Coliseum in Oakland. I saw a bunch of people with my car there, it was cool.

On the way back to Sacramento, I started noticing a whining sound coming from the turbo. Everytime the turbo started spooling, it would start whining. A sound more like a supercharger than a turbo. I drove up to Sacramento, and started asking people on the List to try and figure out what the deal was. The common consensus was that my turbo was taking a dump. I pulled it out (only the turbo this time), and took it up to Turbo Power in Cameron Park by El Dorado Hills.

Dobie and Stacey were the nicest people. Dobie took the turbo apart and let me watch while he took the turbo apart. Pretty simple but there's a lot of accuracy required when you put it back together. I wouldn't recommend it for the do-it-yourself guy. Dobie uses a $7,500 machine to check the balances on the turbos that he rebuilds.

After pulling the turbo apart, it turned out that the bearing at the exhaust side was oil starved. We talked about my set-up and his theory was that the oil velocity was causing the oil to get extra foamy and to block off liquid oil from getting to the bearing at the other end of the turbo.

I have 1/4" steelbraid hose feeding the turbo, but the fitting at the turbo itself (off a Mazda MX-5 Turbo) is really small. He said that the drastic drop in the diameter of the feed line probably caused the oil to shoot out of the fitting at a high speed causing the extra foaming.

That foaming blocked one of the oil passages in the main housing of the turbo, thereby starving the bearing at the other end of the housing. I was told to either move the small fitting further away from the turbo so that the oil had a chance to slow back before the turbo, or use a bigger fitting that he gave me, along with a bigger drain fitting that he also gave me.

Well, being the typical car-guy that I am..."while it was out," I decided to hybrid the turbo...hehe. I went to a bigger impeller housing and bigger impeller blade. Dobie told me that the turbo would build max boost sooner and easier. Two days later, and $300 poorer, the turbo was back in after a few minor adjustments (the drain fitting's angle had to be bent a little to clear the manifold).

It's all in, I'm boosting at about 5.5 psi. I'm waiting on an Autometer oil pressure gauge that I'm going to install at the turbo so I can know everything is peachy keen and happy there. I'm getting puffs of smoke between shifts, but I can live with that. My downpipe is still not perfectly flat, and I'm still getting little exhaust leaks there (and probably from the upper portion of the downpipe that wasn't replaced at Muffler Tech). But it's in, and I'm boosting.

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UPDATE: 4/23/99

This sucks. I was going to Home Depot to see if I could find a check valve. I need one to put at my blow off valve (BOV) because I have an air flow meter (AFM) in the car. It seems that when the car is idling, the vacuum pressure is enough to hold the BOV open. Since all air that goes into the motor has to be metered in the AFM, the car doesn't idle if there are any leaks.

The other solution is to hook up the BOV the "proper" way, which is to re-route the air that is released from the BOV, back into the intake piping before the turbo, but after the AFM. I didn't know it was going to be like this, so I didn't build my kit with those considerations. Modifying everything to do this would be a real pain in the butt.

So, even though it's actually better to re-circulate the air, I'm not going to do it. Hence, I was looking for a check valve so that the valve would be closed when the BOV is open at idle, but will open when it releases air.

Anyway, I was at a stop light after not finding what I needed at Home Depot, and the car started idling really really rough. I pulled into a parking lot, and checked it out. Nothing seemed wrong, but it felt like it was idling on three cylinders, and the power was GONE.

It seemed to come and go as I hit bumps, etc. I think it might be a bad plug wire. I'll change those and see what happens.

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UPDATE: 5/2/99

While I was messing around with the motor trying to figure out why it started idling and driving so poorly while coming back from Home Depot, I broke a temperature sensor at the base. I went to the junk yard and got another one. Then I put in the new wires, and while I was messing around with everything before i drove it, I noticed that the cause of the severe missing seemed to be the AFM or the piping.

Since I went to a bigger filter than my original one that I used when I was fitting everything together, I really had to mash everything under the hood to make it all fit. The result was a pretty tight "kink" in the intake pipe (flexible high pressure piping I snagged off my friend's Jackson Racing Supercharger Kit for his '96 Civic).

After driving the car around the block, the car is missing under boost, and when I got back to the parking lot of my apartment, the temperature gauge was pinned at the hot side. I tripped. I dunno what the deal is now. Everything was fine, until that AFM incident with the rough idle and loss of power. I'm pissed that all I had to do was adjust the piping and everything was okay...now all this.

After putting up my problems to the Toyota-Mods List, I was told that the temperature sensor I replaced has nothing to do with the gauge, etc. I might have the wire right next to it shorted out somewhere (because the motor didn't seem "hot" when I came back...but the needle was pinned). I was told that if there is a short, it'll cause the needle to get pinned.

I'll check that next. I'm also going to take out the filter so there is more room, and I'll try to straighted out that kink to see whether that's causing the misfire under boost. I'm also going to put the old plug wires (NGK) back in since the car was working okay with those before. When I replaced the NGKs, I just used the old OEM wires that I had saved for emergency.

I may tinker with the air/fuel mixture too, if I find that that may be a problem. I was told that I may be running so rich that it's causing the misfire. I'll change the plugs first, take out the kink in the intake, and check the wire to the temperature gauge to make sure it's not grounded to anything. Hopefully that'll solve everything, and I can focus on making a better path for the intake so everything isn't so cramped.

I may move the battery to the trunk. Then the intake filter would be right at the turbo with about 1/4 of the length piping that it currently uses. I'd just have to extend the wiring that goes to the AFM. I don't know if my trunk has the room though. I've got an 8" speaker tube, amplifier, an a rear tower brace back there already.

Oh well...gotta' get to my final now...check back for more updates about my 4A-GTE Corolla.

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UPDATE: 6/1/99

Dunno what the deal is. My car won't start. I've had a few problems with the car dying out on my while driving. I think it may be the ignition system or the fuel pump. I don't have time to tinker with this since I'm studying for finals...it'll have to wait.

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UPDATE: 7/15/99

Well, car starts for about 1-2 seconds and dies off. Still don't know what the problem is. Bar Exam comes up in about two weeks. This will have to wait.

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UPDATE: 7/30/99

Exam's over and the car is fixed. My friend just bought a used MR2 MkI, and he suggested (as well as someone off the Toyota-Mods List) to try the fuel system relay. I pulled out my relay, plugged in my friend's, and VAROOOOM!!! Stan's in business!! I'm sure glad it wasn't the fuel pump or the ignition, that would have been expensive. And here I was ready to bring the car in to a mechanic to troubleshoot. I'm lucky.

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UPDATE: 8/10/99

Car runs well, except that it's sucking big time gas. I went to the local Pick and Pull, and picked up (4) RX-7 n/a fuel injectors. Talk on the List is that these will bolt straight in, and flow more than the stock 4AGE injectors. I'll post the results when I have time to put them in.

Hooked up the BOV today also. Running a long rubber tube to recirculate the released air back behind the air flow meter. It idles and runs fine, but I don't think it's working. I don't hear any "whoosh," when I lift off the throttle.

The problem might be that I'm not making enough boost (5.5 psi) to activate the BOV. It's been so long, but I think I ordered a 6-12 psi BOV. I've been advised that I might want to fabricate a shim to allow lower boost adjustment on the BOV. I'll give that a try since the BOV still isn't opening with the adjustment screw all the way loose (supposedly 6 psi).

I sometimes hear the BOV faintly. These are times when I really mash the throttle. I think in those times, I might be making barely 6 psi, which is enough to activate the BOV.

Oh Yeah, got an OEM Limited Slip Differential a while back and forgot to post an update about it. If you decide to do a conversion from the open diff to the locking diff, make sure you get the LSD axleshafts, they're shorter, and the open diff axleshafts won't fit.

Otherwise, it's a simple swap. Drain the diff housing, pull out the axleshafts, drop the third member, put in the LSD parts, and refill it with LSD fluid. Then you're all ready for 180s, 360s, donuts, or some racing.

I've also gone to the local Pick 'N Pull and snagged four Denso fuel injectors out of a second generation normally aspirated RX-7. Members on the Toyota-Mods List say that they'll drop straight in, and flow quite a bit more than stock. All I should have to do it tinker with the air flow meter to get it to idle properly. I'll probably wait until after smog to put these in.

I bought my parents car off them when they bought a new car. I decided that since I'm always working on my Corolla there was too much downtime and sometimes I would have to borrow my friend's cars. Since I have another main car now, I've taken the first steps to stripping the car out. I took out the radio, amp, and subwoofer and put it in my other car. Little by little, I'll turn my Corolla into a race-only car.


CLICK HERE FOR THE FINAL UPDATE ON PROJECT X


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